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- Juan SkinnerParticipant
I’m not sure what this thing is for exactly, possibly it’s to measure exhaust emissions as the exhaust has a catylitic converter. It is a ten millimetere fine thread blanking screw
It does not restrict gas flow as such, but just taps into the downpipe.
I wonder if anything can be done with a standard pipe to unblock it
Tone.Juan SkinnerParticipantHey I’ve sussed it!
There’s this little blanking screw which is in the exhaust right near the exhaust port. I took is out and went for a spin. Hey presto, power is restored. Makes me sound like a right jonny boy but I think it proves a point – it’s my exhaust bunged up! Gives me a good excuse to get a nice stainless job for it.
Tone.Juan SkinnerParticipantHey, i turns out I was wrong about the unit, it’s called a lighting regulator unit and does, as far as I can see, alternator field current, rectification and flashers but not as I originally thought cdi.
The cdi is actually built into the coil which is why I couldn’t find the bugger in the first place.
The battery is 12v gel type and spins the motor over very well over an extended period so I don’t suspect this could be a problem.I take your point though, on my CB125 import, it was cutting out on what I thought was the overrun. Thinking on, this is when the brakes are applied. 21W bulb brought into circuit, nearly 2A drain from the battery and the result is weak sparks. The battery is new, and I’ll check tomorrow but I suspect it’s not charging.
Back to the scooter, it’s getting worse day by day. When I go on a test run, people are now swearing and gesticulating at me as if I’m trying to piss them off. If only they knew who was *really* pissed off. As it degenerates, it is obviously missing, going in fits and starts on full throttle.
A new cdi/coil is £45 which is fine if it solves the problem. If not I’ll be £45 worse off and still have the original problem.
My only reservation is that I do not have a timing light. Can anyone recommend a good basic (active not passive) one? I swore an oath against petrol engines being a diesel head by nature but I forgot all about bikes. Bad mistake to make.Regards,
Tony.Juan SkinnerParticipantI thought 409 was the basic stuff, 304 is better and 304L is better still.
Is 409 is not used anymore for exhausts?
Tone.Juan SkinnerParticipantOh if only it were that simple! Of course your right, the plug would have looked chalky if this were the problem. When I finally found my T30 Torx
tamperproof driver bit and took the duct off, it appeared split but not enough to penetrate right through. A healthy blob of plumbers silicon sealant was
gobbed around it just to be sure. It still ran completely gutless, worse when the throttle was wide open and worse as it got warmer.
I had checked the automatic choke. Although the carb is plumbed into the coolant, my assumption now is this is just a de-icer. Had me thrown for a while.The carb is a DellOrto PVHA and the automatic choke is done instead by an element heated by the lighting coil which extends a brass rod, acting as a slide
valve, to cut off a bypass drilling and associated choke jet. It showed a good low resistance and extended from 11mm when cold to 14mm after a couple of
minutes.
Next, I’m going to go for the sparks side of things. It’s a bit of a pig because getting at the module involves taking off loads of plastic. The module doescdi and a whole bunch of other things such as flashers. My indicators have spates of flashing very fast, as if a bulb has gone but it happens both sides and
all four bulbs are fine. This unit has always been under suspicion.
One fine day, I’ll get out of this boiler suit and go for a very enjoyable raz, till then I’m still scratching my head over this one.
A little about the bike
This NRG 50 liquid cooled, dual disk brake bike has a bit of history behind it. It was bought originally by a millionaire as a pit bike for the gumball
rally. He had it derestriced, keeping the original pipe but blanking off the resonant tube. I guess the variator nylon washers have been removed but I can’t
find any other modifications.
Tone
Juan SkinnerParticipantGrr, yes the plug would have looked chalky I guess. I had the inlet duct off and it was quite deeply split but not all the way through. A good blob of silicon sealant was applied just to eliminate any doubt but sadly, this wasn’t the cure. I did notice though that there was what looked like drops of water right on the reed valve. The bike is the liquid cooled version btw. The crankcase had some fluid swishing about in it, perhaps only 1cc of the stuff but i’ve never seen a 2 stroke crankcase looking this wet. It had a viscosity more like oil than water and there was no sign of rust on the crank.
Next thing I suppose is to look at the ignition circuit. This is a pig because loads of plastic has to come off to get at the cdi box.
It’s all done in one unit, cdi, flashers et al. My indicators often start blinking fast so this unit has been suspect for quite a while now.
I’m hoping to get these overalls off one day and go for a proper raz without having to push it up hills!
Tone.Juan SkinnerParticipantUpdate:
I blanked off the EGR and found it made no discernable difference.
I’ve found a crack in the rubber inlet duct between the carb and reed block.
Not sure if it goes right through but its my prime suspect at this stage.
Tone.Juan SkinnerParticipantColin Fitch tells me that they fabricate exclusively in 304.
Sounds good to me
ToneJuan SkinnerParticipantWell I hadn’t, but I have now. Thanks very much. That looks a very decent system indeed and not many more £££s than the mild steel BSM product that I wa previously considering.
I’ve emailed them to ask what grade of SS they use and if they can make it in 304 grade.
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